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UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF NUCLEAR REACTOR REGULATION WASHINGTON, D.C. 20555 May 24, 1994 NRC INFORMATION NOTICE 94-36: UNDETECTED ACCUMULATION OF GAS IN REACTOR COOLANT SYSTEM Addressees All holders of operating licenses or construction permits for nuclear power reactors. Purpose The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to alert addressees to problems that could result from unrecognized evolution and accumulation of gas in reactor coolant system high points. It is expected that recipients will review this information for applicability to their facilities and consider actions, as appropriate, to avoid similar problems. However, suggestions contained in this information notice are not NRC requirements; therefore, no specific action or written response is required. Description of Circumstances Sequoyah Unit 1 had been shut down in March 1993. In early September 1993, after the unit had been refueled, the reactor vessel was reassembled and the reactor coolant system was degassed, filled, and vented. The reactor coolant system was then depressurized to atmospheric pressure. One pressurizer power-operated relief valve (PORV) was open and the reactor coolant system average temperature was being maintained at approximately 49C [120F]. Nitrogen cover gas was being supplied to the volume control tank at approximately 239 kPa [20 psig] and reactor coolant was being circulated by the charging system and the residual heat removal (RHR) system. The reactor vessel level indication system (RVLIS) was functional for a significant portion of the event. Before this event, instrument maintenance stickers were placed on the RVLIS indicators for other maintenance work. Although the RVLIS information was available, the operators were not monitoring this information because it was not procedurally required to be used in shutdown modes of operation. Reactor coolant system inventory was being monitored using pressurizer cold calibration level indications. On December 17, 1993, the operators began to pressurize the containment to 191 kPa [13 psig] in order to perform a containment integrated leak rate test. As containment pressure increased, the operators noticed a decrease in pressurizer water level and, over a period of time, added approximately 31,400 liters [8,300 gallons] of water to maintain the pressurizer level. Licensee personnel evaluated this situation and recognized that gas was accumulating in the reactor coolant system. However, they failed to recognize the magnitude 9405190137. IN 94-36 May 24, 1994 Page 2 of 4 or cause of the problem. Three days later, as the containment was being depressurized upon completion of the containment leak test, the operators noted that approximately the same amount of water had to be removed from the reactor coolant system to maintain the level. On December 21, 1993, on the basis of operators' observations of the changing coolant system inventory during the containment leak test, the reactor vessel head was vented. It was subsequently vented several times to maintain appropriate reactor vessel inventory based on RVLIS information. The reactor vessel gas voiding conditions went undetected from early September 1993, when the reactor coolant system was verified to be filled, until December 21, 1993, when the reactor head was vented. The gas evolution resulted from the temperature in the volume control tank being much lower than that normally expected. (This lower temperature was due to unusually low component cooling water temperatures and to a maintenance problem with a cooling water valve that resulted in the reduction of the heat sink temperature in the letdown heat exchanger.) The lower temperatures increased the solubility of gas in the volume control tank water so that more gas was dissolved in the water. This gas evolved when the water was transferred to the reactor coolant system by the charging system and heated up in the reactor vessel. Further details concerning this event are in NRC Inspection Report No. 50-327; 50-328/94-04. Discussion The licensee completed a final evaluation in January 1994 and determined that during this event the reactor vessel water level had decreased to slightly below the top of the hot leg, and that the steam generator tubes were nearly empty. The reactor coolant system inventory was being monitored solely on the basis of pressurizer level, which was not indicative of the reactor vessel and steam generator levels. Calculations by the licensee indicated that an equilibrium had been reached during the event so that the water level was approximately 1.6 meters [5.25 feet] above the top of the core. Any additional gas evolved in the reactor vessel would be expected to be vented through the hot leg and surge line to the pressurizer and out through the open pressurizer PORV. The reactor water level at which equilibrium was established at Sequoyah was sufficiently high so as not to interfere with reactor coolant flow through the RHR cooling system. However, at other plants, the equilibrium level, which is related to pressurizer surge line geometry and RHR suction line location, might be such that a similar event could interfere with shutdown cooling. Another potential safety concern is related to the capability of the steam generators to transfer heat from the reactor coolant to secondary coolant. In the equilibrium condition at Sequoyah, the steam generator tubes were almost empty during at least a portion of the duration of this event. During this. IN 94-36 May 24, 1994 Page 3 of 4 period, the steam generators were assumed to be available as an alternate means for shutdown cooling. It is not clear that cooling through the steam generators could have been established, if needed, especially because the plant operators were unaware that the tubes were empty. Several factors involving licensee performance contributed to the delay in the identification and evaluation of this event. They included (1) lack of consideration on the part of licensee personnel with respect to compression of gas in the system caused by containment pressure transmitted to the reactor coolant system water through the open pressurizer PORV; (2) misunderstanding by the operators about the operability of RVLIS; (3) failure to stop the containment leak test when water level changes were first noted so that the situation could have been adequately evaluated; (4) an apparent lack of thorough evaluation of previously published information on similar events. The event discussed in this information notice highlights the potential for gas evolution and accumulation in the reactor coolant system in locations and quantities that may not be evident to operators. Changes in temperature and pressure can have significant effects on the solubility of gas in water, especially at or near atmospheric pressure conditions. During cold shutdown, this phenomenon can permit significant quantities of cover gas to be dissolved in lower-temperature, higher-pressure volumes such as the volume control tank and to evolve into a large gas bubble in the reactor vessel (a lower-pressure, higher-temperature area). This phenomenon can occur without a sudden change in pressurizer level, which is the indicator normally used by the operators to monitor water inventory. Use of available instrumentation in shutdown modes to monitor reactor vessel water level can provide detection of unexpected system conditions when reduced vessel inventory is not planned as well as in reduced inventory evolutions. On April 12, 1994, a similar gas accumulation event was identified at the Salem Generating Station (Unit 1) shortly after it entered Mode 5 (cold shutdown) operation. Although this occurrence did not involve amounts of gas accumulation as large as in the Sequoyah event, many similarities existed regarding both the process of gas formation and the lack of operator awareness of the abnormal condition. In both events, reactor vessel level information was or could have been made available for prompt identification of the problem. Related Generic Communications NRC Information Notice 93-12, "Off-Gassing in Auxiliary Feedwater System Raw Water Sources," discusses similar solubility considerations related to air pockets in piping at the McGuire Nuclear Station. NRC Information Notice 87-46, "Undetected Loss of Reactor Coolant," discusses undetected loss of reactor coolant inventory at North Anna Unit 1 resulting from inadequate use of available indications and failure to perform mass inventory balances. . IN 94-36 May 24, 1994 Page 4 of 4 This information notice requires no specific action or written response. If you have any questions about the information in this notice, please contact one of the technical contacts listed below or the appropriate Office of Nuclear Reactor Regulation (NRR) project manager. /s/'d by BKGrimes Brian K. Grimes, Director Division of Operating Reactor Support Office of Nuclear Reactor Regulation Technical contacts: R. Benedict, NRR (301) 504-1157 S. M. Shaeffer, RII (615) 842-8001 Attachment: List of Recently Issued NRC Information Notices
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